MEO Provides Update on Gurame SE-1X Well, Indonesia

MEO Provides Update on Gurame SE-1X Well

MEO Australia announced update in relation to Gurame SE-1XST being drilled in the Seruway PSC, offshore North Sumatra.

Since the last report, wireline logging operations were completed over the Baong sands. A 7” liner was run and cemented to 2,961mMDRT. At 0200 hrs (local time) the rig was running in hole preparing to drill out of the 7” liner.

Logging results coupled with gas shows while drilling indicates the Baong sands are gas saturated. Image logs show the Baong sands to be finely laminated with significant fracturing. A dual packer MDT was run which confirmed the reservoir has matrix permeability. MEO has elected to production test the Baong sands to determine gas composition and reservoir productivity and has secured $10 million to fund this testing program.

The forward program is to drill out of the 7” liner and into the second primary target, the Belumai sands, prior to production testing the Baong sands.

MEO’s CEO and MD Jürgen Hendrich commented on the announcement: “The decision to production test the Baong sands represents a significant investment. We are very pleased to have secured a substantial shareholder and funding for this undertaking.”

[mappress]
LNG World News Staff, November 19, 2012